油气藏评价与开发 ›› 2021, Vol. 11 ›› Issue (2): 230-234.doi: 10.13809/j.cnki.cn32-1825/te.2021.02.013

• 页岩气开发 • 上一篇    下一篇

深层页岩气井压后井筒堵塞解除技术——以WY23-1HF井为例

王孝刚(),史雪枝,朱敏   

  1. 中国石化西南油气分公司石油工程技术研究院,四川 德阳 618000
  • 收稿日期:2020-11-05 出版日期:2021-04-26 发布日期:2021-04-30
  • 作者简介:王孝刚(1979—),男,硕士,高级工程师,主要从事气井完井测试及井下作业的设计和科研工作。地址:四川省德阳市旌阳区石油工程技术研究院,邮政编码:618000。E-mail: 463848973@qq.com
  • 基金资助:
    中国石化科技部项目“深层页岩气高效钻完井技术”(P18058-2)

Plugging removal technology of wellbore after fracturing in deep shale gas wells: A case study of Well-WY23-1HF

WANG Xiaogang(),SHI Xuezhi,ZHU Min   

  1. Research Institute of Petroleum Engineering, Sinopec Southwest China Oil and Gas Company, Deyang, Sichuan 618000, China
  • Received:2020-11-05 Online:2021-04-26 Published:2021-04-30

摘要:

深层页岩气井大规模体积压裂后,面临井筒堵塞影响长期生产的问题,需借助连油或钻杆进行解堵处理,处理方式较为单一,对于复杂变径井筒、混合堵塞物问题的处理缺乏针对性。以WY23-1HF井为例,该井受邻井压裂影响无法正常生产,地层垮塌,岩屑进入井筒造成了严重堵塞,同时,堵塞段存在轨迹上翘、套管变形等复杂情况。解堵复产措施包括:钻磨管柱、钻磨工序、压井液设计等方面。现场实施情况表明,针对水平井多段压裂,应尽量采用同一类型桥塞减少变径影响,确保轨迹平滑和防止堵塞物堆积,避免井筒条件复杂化,同时,结合该井可溶桥塞与大通径非易钻桥塞混合使用的情况,采用连油带笔尖冲洗+钻杆带钻头(或磨鞋)的管柱组合,进行通磨钻扫相结合成功实现复产,为类似的页岩气井提供借鉴。

关键词: 钻磨桥塞, 堵塞, 解堵, 复产, 水平井, 页岩气

Abstract:

After large-scale volume fracturing of deep shale gas wells, there comes the difficulty of wellbore plugging, which affects long-term production. The common methods to remove the wellbore plugging by coiled tubing and drill pipe are simple. It lacks of the pertinence measures to treat the diameter shaft and the mixed stemming. For example, Well-WY23-1HF can not produce normally due to the fracturing of adjacent well. The formation collapses and the cuttings enter the wellbore, causing serious plugging. The trajectory of its plugging section is of the complex situation of warped, casing deformation and so on. The measures of plugging removal and resuming production are drill-grinding string, drill-grinding process, well killing fluid design, etc. The field application shows that the same type of bridge plug should be used to reduce the impact of tapering, ensure the smooth trajectory, prevent the accumulation of plugging material, and avoid the complication of wellbore conditions for multi-stage fracturing of horizontal wells. At the same time, combined with the comprehensive application of soluble bridge plug and large diameter non-easy-to-drill bridge plug, the combination of pipe string with oil flushing with nibs+drill pipe with bit (or milling shoe) is adopted to remove plug, and the recovery of production is successfully achieved. This technology provides a reference for similar shale gas wells.

Key words: drilling bridge plug, plugging, plugging removal, recovery production, horizontal well, shale gas

中图分类号: 

  • TE37