油气藏评价与开发 ›› 2023, Vol. 13 ›› Issue (4): 416-423.doi: 10.13809/j.cnki.cn32-1825/te.2023.04.002

• 煤层气 • 上一篇    下一篇

新型排采泵在延川南深层煤层气井的改进及应用

吴壮坤(),张宏录(),池宇璇,印中华,张壮   

  1. 中国石化华东油气分公司石油工程技术研究院,江苏 南京 210019
  • 收稿日期:2023-01-30 发布日期:2023-09-01 出版日期:2023-08-26
  • 通讯作者: 张宏录(1966—),男,本科,高级工程师,主要从事采油气工艺的研究及推广工作。地址:江苏省南京市建邺区江东中路375号金融城9号楼,邮政编码:210019。E-mail:2534032617@163.com
  • 作者简介:吴壮坤(1972—),男,本科,高级工程师,主要从事非常规油气资源勘探开发与科研生产工作。地址:江苏省南京市建邺区江东中路375号金融城9号楼,邮政编码:210019。E-mail:uzk.hdsj@sinopec.com
  • 基金资助:
    中国石化科技项目“低压煤系气藏地质工程一体化高效开发技术”(P20074)

Improvement and application of a novel drainage pump of deep coalbed methane wells in south Yanchuan

WU Zhuangkun(),ZHANG Honglu(),CHI Yuxuan,YIN Zhonghua,ZHANG Zhuang   

  1. Engineering Design & Research Institute, Sinopec East China Oil and Gas Company, Nanjing, Jiangsu 210019, China
  • Received:2023-01-30 Online:2023-09-01 Published:2023-08-26

摘要:

针对延川南煤层气田因地层出煤粉导致机抽井频繁躺井作业的问题,开展了延川南煤层气井新型排采泵的改进及应用研究。新型排采泵游动凡尔设计为强制拉杆半球式密封,柱塞总成采用中空设计,泵径ø38 mm,冲程3.0 m,冲次1~3次/min,排量4.8~14.6 m3/d。新型排采泵与空心杆、油管配合使用,从而形成了生产和洗井双通道一体化管柱。既能满足正常的排水采气生产,又能实现洗井排煤粉的需求,而且洗井时洗井液不进入地层,避免了洗井液对地层的污染,实现了不起管柱作业并将煤粉从井中排出,解决了煤层气田排采井煤粉或砂粒沉积导致的固定阀失效和卡泵的问题。2022年,新型排采泵在延川南煤层气田开展了2口井现场应用,实施后没有发生固定阀失效和煤粉卡泵,措施井平均检泵周期延长285 d。现场试验表明:新型排采泵具有正常排水采气和通过洗井将煤粉从泵中排出双重功能,为延川南煤层气田防煤粉工艺提供了一种新的技术支持。

关键词: 煤层气, 排水采气, 煤粉卡泵, 新型排采泵, 检泵周期

Abstract:

In order to solve the problem of frequent well laying in the coalbed methane field in south Yanchuan due to sand production(pulverized coal), a novel drainage pump in south Yanchuan coalbed methane well has been developed. The novel drainage pump is designed as a forced pull rod hemisphere-type seal, and the plunger assembly adopts a hollow design. The pump diameter is ø38 mm, the stroke is three meters, the stroke time ranges from one to three times per minute, and the displacement is 4.8~14.6 m3/d. The novel drainage pump is used together with hollow rod and tubing, forming a dual-channel integrated pipe string for production and cleaning. It can not only meet the normal drainage gas production, but also facilitates well flushing and discharging pulverized coal. In addition, the flushing fluid does not enter the stratum during well flushing, avoiding the pollution of the flushing fluid to the stratum and preventing the failure of the fixed valve and the pump from being stuck caused by the deposition of pulverized coal or sand in the coalbed methane field drainage well. In 2022, the novel drainage pump was applied in two wells in the south Yanchuan coalbed methane field, and since then, no fixed valve failure or pulverized coal card pump has occurred. As a result the average pump inspection period of measure wells has been extended by 285 days. Field tests demonstrate that the novel drainage pump has the dual functions of normal gas drainage and coal powder discharge through well flushing, providing a new technical support for improving the overall development level of coalbed methane field in south Yanchuan.

Key words: coalbed methane, drainage gas production, pulverized coal stuck pump, novel drainage pump, pump inspection cycle

中图分类号: 

  • TE37